pleased to say I got it working today on all accounts. it did take several tries however.
I'm now using my 'config 3' (see above) with an improved heatsink and fan design to blow the warm air down onto the bed to help with bridges etc. this is necessary since I've hooked the fan up to where the original cooling fan went but I still want to have bridging capability.
I got a bottle brush, drill, and some polishing paste and went mad polishing the inside of the nozzle and stainless steel section. they were already well polished and I'm not sure I opened up the ID much if any, but it made me feel better.
anyway it prints NYLON at 280C and it prints it well. the cold end is cold enough to touch (I would guess 40C) so will be OK for PLA also.
I need to tweak all the slicer settings big time, getting layers to stick is hard, edges are a bit wobbly right now and infill is a mad squiggly mess.
I also printed at 150% extrusion to stress test. no leaks, a little bit of burning smell (I think it was the heatsink compound), no pops (since it's not possible anymore!) and a constant stream of 0.6mm material (from a 0.4mm nozzle).
oh. and did I mention the NYLON and the 280C, no more PEEK for me!
(hey maybe I can extrude PEEK, that might be fun)
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I'll second that. and probably a carbide bit is a good idea anyway. the work hardens very easily and then becomes impossible to drill - I found going slow was a really bad idea on some test pieces.
I've ordered some carbide bits and a reamer too for good measure, I'll see what happens if I open the tube out by 0.1mm.
meanwhile I now have a config 3 - E3D nozzle, E3D SS section, UM V1 heater block and heater, E3D cooler block. This is a totally V2-less solution for those wanting to go straight from V1 to V3. I've improved the fan design slightly and will post some pics shortly. I think I'll stick with the 'hanging' bowden solution since it seems to work better than expected. (I can even get the calipers in there or a marker pen to color the filament as it goes into the nozzle!)
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